Click here for the summary of the ordering
process. 5-4-02: This weekend I installed the intercooler,
replaced the lower intake gasket, re-torqued the head studs and installed the
new 42# injectors and Pro-M MAF. Everything went suprisingly well.
Based on my friend Scott's recommendation we took the whole front clip off for
the install. He said it was easier this way when he did the intercooler on
his Procharger. Scott had the whole front clip off in about 15
minutes!
The bolt holes on the intercooler lined
up perfectly to the bumper supports. However the intercooler does sit a
bit close to the 5 mph bumper supports. If I get into the slightest fender
bender the intercooler is going to be trashed. There were also some
modifications that had to be made to make it fit, but I was expecting that
because that is true of all intercooler installs. First, my friend Mike
had to clearance the plastic bumper support in two places as you can see in the
photos where it was rubbing. Also two of the screws that hold this bumper
support into place had to be either shortened or left out all together.
You can also see that in the pictures. We also had to cut some of the GT
front fasica out in order to make it fit correctly. I also left out the
large fog light bracket. The thing weighs a ton and it was only getting in
the way. Besides, I don't even have foglights so I don't care. I
think that leaving this bracket out actually offset the extra weight of the
intercooler, I was happy about that since my car is a fat pig anyway.
| Plenty of clearance
here. |
Plastic will need to be
trimmed... |
on both ends |
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| Very close to the 5mph crumple
area. |
this bolt will not go through, the
hose is in the way. |
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| Scott, hard at work. |
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5-10-02: My friend Kyle was able to get his boss's shop for
the weekend so we could use the lift to swap oil pumps on my car. I bought
my current 306 from a friend and it already had a melling high volume pump on
it. However this pump is putting out way too much pressure for a
turbo. In fact I have blown the seal on two oil filters!! Since then
I have put in a $10 K&N oil filter and it hasn't popped. However I am
afraid it will tear up the turbo seals. When it is cold the oil pressure
bottoms out my 100 psi gauge, so I have no idea how high it is actually
getting. When it is warm I see 60 psi. I am installing a Melling
standard oil pump. Also at this time I am going to punch and tap the oil
pan for the oil return line.
The oil pump
install went ok and punching and tapping the oil pan was no big deal. We
used about a .420 tap and it worked fine with the supplied fitting by
Cartech. Swapping oil pumps took a few hours and we did it with the engine
in the car and without removing the steering rack. It definitely
wasn't fun. We also installed a T-rex fuel pump from Vortech. The parts
list and instructions were AWESOME for this pump. It is really
unbelievable how well it went in. They even supply a handy little template
for drilling holes in your trunk area for the mounting brackets! Big
thanks to Kyle for all his help, Kyle is the man!
| Shot of the trimming we did a week
before. |
Oil pan hole |
Kyle at 2am. |
Got JB Weld?? We
do! |
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| T-rex installed. |
Putting in new oil pump. |
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5-11-02:
After the fuel pump install I drove the
car home and started tearing it apart. I took the longtubes and x-pipe
off. Good riddance to those things! I bolted on the passenger side
header from Cartech which is a JBA shorty. It went on really easy.
Then I worked on the passenger side intake piping. This is
where I realized that the supplied connecting hose for the piping to the
70mm throttle body would not work. Lastly, I did some other
small stuff then I went to bed.
5-12-02: My friend Jim showed
up today to help with the install. He has a T-72 cartech kit of his own so
he has a lot of knowledge on this stuff. First we re-located the
powersteering pump with the supplied bracket and fittings. It was really
easy and only took about 20 minutes. Next we started on the turbo
header. Now is where it gets bad. First we tried bolting it on but
we soon realized that some of the bolts just will not go into the holes. I
probably should have checked this weeks ago, but I didn't. So we had to
take the header off and try to clearance the tubes so the bolts would fit.
All we had was a hammer and a bolt, no torch. So we spent about 30 minutes
hammering on the tubes. That gave us just barely enough room to
procede. From there we put the header on by barely starting two of the
bolts. Then you have to gradually tighten 3 of the bolts a little at a
time, or else they will go in sideways. Jim worked on tightening that
thing for at least 2 hours. What a MAJOR pain in the butt!!
Next we trial fitted the turbo to
mark the hole for the inlet pipe that we would be cutting with a hole saw.
The turbo cleared the frame and the sway bar mount by a long shot so the only
cutting we will need to do is for the inlet pipe. My friend Mike showed up
with a brand new drill for me! Unfortunately the power packs come
uncharged so we never had time to charge them up enough to cut the hole all the
way.
Next was the crossover pipe. Jim
started on the passenger side pipe then tried attaching the longer piece that
goes over to the turbo header. To make a long story short, it appears that
the smaller passenger side piece was welded together wrong and the big driver's
side piece is hitting the steering shaft and it is hitting all over the lakewood
bellhousing. So I will be having the car towed to a custom exhaust shop to
fix the crossover pipe.
During this time I also trial fitted the
intake piping from the turbo to the intercooler. Everything seems to fit
ok but the S-shaped pipe where the BOV mounts is at a funny angle to the turbo,
but it looks like it will work just fine. The radiator hose also fits
nicely, I had to go and buy one with larger openings since I have a universal
fit Ron Davis radiator, but that is to be expected.
Lastly we put together the fittings for
the oil system, there are a lot of fittings involved, but Jim put something
together that would work and still clear the downpipe and everything else.
This is where we realized that the turbo drain plate that we have was drilled
for a larger fitting that we do not have. Cartech is sending me a larger
fitting.
Little stuff: When
they made my MAF bracket they forgot to send some "turbo" hose to connect the
pipe to the turbo and to the MAF. Mike is also sending me some pieces of
hose so I can complete the install. Also keep in mind that the kit is
designed for a stock mustang with a stock throttle body. The supplied
hose will not go onto a 70mm or larger throttle body. Another thing is the
little stud on the downpipe that is used to attach a bar to in order to keep the
pipes together. This little stud is hitting the motor mount and barely
keeping the downpipe from lining up correctly with the turbo.
5-14-02: I picked up my car
from Pro Dyno today and they did an excellent job on my exhaust. They
fixed the crossver pipe and they made a custom 3" Y-pipe that goes from the
downpipe to my mufflers. Those guys rule.
Once I got the car home I put in the new turbo drain
that Mike overnighted to me and it fit nicely. Then I completed the hole
in the fender for the inlet pipe. We also extended my MAF wires and worked
on re-wiring the jungle of wires on my fender where the turbo inlet goes.
Kyle also got my oil pressure gauge installed. All that is left to do is
get the downpipe to bolt up and button everything up!!
5-15-02: When I put the turbo
on for supposedly the last time I soon realized that the turbo drain was inside
the frame rail and there was no way to get a hose on it. So my friend when
to Ace Hardware and they do not sell any 45 degree fitting in the style we
need. So I got a 90 degree. With the 90 installed I still had
clearance problems, so I had to notch the frame for the turbo drain. After
that was done I thought I was again putting the turbo on for the last time,
wrong again. The bottom bolt on the turbo on the driver's side is
impossible to put in. As it turns out my header is supposed to be studded
here. It was too late to go to the parts store again... During this
time I also got the oil dipstick tube in. This was fairly difficult
because the downpipe is right against the engine block. I had to pry the
pipe away from the block and slide the tube in.
5-16-02: I made some studs
today and I threaded them into the header and slid the turbo on.
Unfortunately the nuts are TOO BIG to clear the exhaust housing! This
is unbelievable. I do not know what they expect you to use on this
thing. So I put the thing together with 3 bolts holding the turbo
up. Next we trial fitted the MAF elbow, which is a PITA to get into the
fender and onto the mounted turbo. We had to take it off and then take
about 2.5" off of the elbow (but MIke told me that the elbow would have to be
cut to fit, it is a custom item). We got the BOV and wastegate installed
next, it is pretty straighforward, however the nuts that mount the wastegate to
the header fit very tight against the wastegate, but it works. After some
more crap we got the car started and I was about to test drive it but we noticed
a huge puddle of oil. We forgot to fully tighten the oil feed line, so we
tightened it and finally I went on the maiden voyage with the car.
Unfortunately it is detonating like crazy even though I am only running 18
degrees of total timing with my tweecer.
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Powersteering
re-location |
Powersteering
re-location |
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| Little did we know this header
wasn't going to seal |
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Drilling hole in fender |
Marked hole |
oil fittings |
more oil fittings |
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| Me. |
Jim F and me |
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| Beau's T76 vs my T64 |
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My T64 assembly |
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| Vacuum routing |
Vacuum routing |
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Psycho Jason |
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Here you see why it takes a stud
and not a bolt |
Semi-finished product. |
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More info: Ok I am going crazy trying to keep
track of dates and stuff so I will just be going off on the past weeks event in
free form. I figured out that the car was detonating at part throttle
because my base timing was at 10 and I did not change any of the base spark
tables in the tweecer. So I set the base to 4 and everything was
super. However I am stil only seeing about 2 lbs of boost. However,
my boost gauge reads 2 inches of vacuum when the car is off, it should be
reading 0. It looks like my gauge is wrong. Later in the week I
tried my friends boost gauge and it showed 4 psi but I have a huge exhaust
leak. Also during the second test drive my clutch cable bit the dust and
while trying to limp the car home one of my fuel lines blew off the fuel
filter. This is because you have to use a hose clamp because that is what
the T-rex install calls for. I need to figure out something better than a hose
clamp. We are having fun now!!
So I tried putting the clutch cable onto the rear
hook of the steeda quadrant and adjusting the firewall adjuster all the way out.
That lasted about 10 feet before the cable came off again...So I get a new ford
cable and everything is great. The clutch pedal is a lot easier now, moral
of the story: do not use cheap checker auto parts clutch cables. There is
a reason the ford motorsport one costs $80 and the checker one is $40.
:) Also after this test drive with the new cable I get a flat tire
somehow. When I get home I notice I have about 6 psi in the driver's rear
tire. So I throw in 2 cans of fix a flat so I can drive it to a
shop...
5-22-02: Ok, so the exhaust
leak has only gotten worse and I have given up. For the first time ever I
am going to take my car to a shop (one that I trust a lot BTW). So I drove
the car to Keith at Street Flight and told him to fix my exhaust leak and to
beat the heck out of the turbo header so the bolts would go in easier. He
also checks the header flange to make sure it is true. So I get there
after work and help him put it back together. We start it up and it is
leaking worse than before and we notice that the bottom of the header is not
sitting against the head flushly. Needless to say I am uber-pissed at this
point. 5-23-02: I get on the phone with Mike and let him know that I am
going crazy. He calls Keith at street flight and they come up witha plan
off attack. Keith is going to mill the flange and cut the flange so it
will give us a little pull with the flange. I get back on the www.theturboforums.com board and I get a
lot of feedback. Most guys say to mill the flange anyway. Then two
people tell me they had the same problem with their AFR heads and the cartech
header. I call Chad in St. Louis and he explains the exact same problem to
me, the solution is to hack a good amount of the flange off below each
port. This way it won't hit the dumbass head. I email Mike and tell
him to call me. In about 30 minutes I am in a conference call with Mike
and Preston from Cartech. I let them know my findings and they are
apologetic and they have never heard of this problem until now. I remind
them to tell this to all the people who call in so that in case they have AFR's
they do not run into this problem. Also at this time I tell mike that my
turbo drain hose was about 2" too short and the heater hose I am using now will
not work for long as it will turn to a gooey mess. He agrees and says that
he has plenty of hose and how much do I need. So he is shipping me another
package. :-) 5-23-02: I get to Street Flight after work and we
finally get the car put back together at 8:30. We cross our fingers and
start the car....we hear a huge exhaust leak again. But it turns out to be
the passenger side flange that we forgot to tighten. We tighten it up and
try again. The car is dead silent, except for a small leak above the #7
port. Keith says we should be able to fix it later. Keith also lets
me know that my tire went flat today....so I am already broke from this and
I am dreading the bill from Keith but he is very fair with me. I highly
recommend him, he is the only person I have ever let work on my car,
until now it was just me and my friends. I drive home and I am seeing
about 5 psi.
I add in a few degrees of
timing @ WOT with the tweecer and go for a test drive...I am getting a
little bit of detonation. Also when I depress the clutch to coast up to a
light the car goes into limp mode and the idle goes from 500-1200 and the check
engine light comes on. When I let the clutch out or come to a stop the
light goes off and the idle returns to normal?? Another thing is at
cruising speeds on the freeway the car is running really rough, as if it is
missing. Then on the way home from the test drive I hear a horrible
grinding noise from the back of the car. I hurry it home and it the sounds
appears to go away when I hit the brakes, so something is wrong with the
brakes.
That is where it stands today, Friday,
5-24-02. This morning I went out to check on the car and the tire
was flat again, life is certaintly sucking right about now.
6-17-02: I havent been very
good about keeping up with this log lately because I am trying not to think
about my car. I am burned out on it right now and I can't afford to spend
anymore money. I got the tire fixed, blew through another clutch cable or
two and I figured out the grinding noise in the rear end was the parking brake
cable hitting the driveshaft. The car is still on the road and it
runs and drives fine. It just isn't making any horsepower. With the
help of Byron Reynolds at www.racesystems.com I was able to figure
out the coasting stalling problem. There is a value in the eec that can be
modified with the tweecer. It is the minimum MAF voltage. Stock it
is set for .2 or something. So if the MAF voltage gets lower than that the
car goes into limp mode and floods the engine. The MAF can see less than
.2 voltage on a power adder car because sometimes there is 0 air passing through
it or air passing through the wrong way! Once I changed this value to 0 my
problems went away. I am also controlling all of the timing functions with
the tweecer. I have modified the WOT timing tables a great deal and I have
also changed all the base timing values. Although I can still get a little
detonation in agressive part throttle situations. But if I keep it at WOT
there is ZERO detonation. This is very strange since my TOTAL timing is
not greater than 20 and I am only running 5 psi of boost.
The car feels very torquey but it is not making much
horsepower. I was having a problem making over 5 psi of steady boost so I
hooked up a manual boost controller. Now it will see 7 psi at lower rpm,
but by 5k it is less than 4 psi, so I have a boost leak or something
somewhere. I have pressure tested the system and I found and corrected
several boost leaks between the turbo and the intake. But there is
still a problem somewhere.
I am very frustrated with the car right now and
chances are I have probably partially blown a head gasket at some point with all
the problems I have had with detonation. I pressure tested the radiator to
check for a blown head gasket and it lost 1 psi after a 15 minute period, so I
might have a partially blown head gasket. The car will make full boost by
2200 rpm which is pretty cool. And the sound of the turbo and the BOV is
really cool, I just wish I had some horsepower.
Well it is obvious that the turbo kit is
fully installed and sort of tuned. So from this point forward I think it
would be appropriate to keep track of my daily log of headaches on another
page. To keep up to date with my car please go here: Living with a Turbo Mustang by
me.
| Here you see the first part of the
custom 3" exhaust. |
3" pipe which Y's to the
mufflers. |
Same pipe. |
THis is what needs to be done to
get the cartech header to fit with AFR heads!!! |
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This is the frame rail so the
turbo drain hose would fit. |
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The non-slip fit crossover
pipe. |
Needs to be cut and welded when I
remove it. |
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Tips for installation:
First, clearance the turbo header so that the
header bolts go through each hole EASILY. This will save you a lot of time
and headaches when you try to install it. Also make sure you have studs
for the lower holes where the turbo bolts to this header. Also make sure
you have the proper nuts that thread onto the wastegate studs on the header
(they are a fine thread) If you have AFR heads
you need to trim the bottom of the flange at each port on the turbo
header!!!!
If you have a bypass valve you will need to make sure
that Cartech send you the proper MAF elbow, also make sure you get the hose
couplings for this elbow. It will be up to you to go to the parts store
and buy some hose that goes from the BOV to this new MAF elbow. I used
some flexible 1-1/8" radiator hose. The elbow that Cartech sends will need
to be cut to fit your Mustang, they make it longer that it needs to be so you
can make it whatever length you need. I had to take about 3" off each side
of it so the MAF and filter would fit in the fender.
When everything is installed make sure the oil
fittings are all tight and everything is away from the turbo and header (clutch
cable, plug wires, O2 sensor wire, etc)
Now you have to route the vaccuum lines. You
will need a vacuum line that goes from the side of the wastegate, there should
be a threaded hose barb that will thread right in. The hose from here will
go to the side of the turbo (it will transmit the boost signal to the
wastegate). If you have a bypass valve you will need to route a vaccuum
line from the manifold to the top of the bypass valve. This will allow the
bypass valve to sense vaccuum.
You will probably have to trim your frame rail so the
turbo drain rail with fit directly onto the bottom of the turbo. Of course
this all depends on what size turbo you buy.
Thanks to all these people who stopped by and helped
in some way: Kyle, Jason, Jim, Croke, Shawn, Brian, Mike and Keith at
Street Flight.
If you wish to give me some feedback or anything at
all just email me: trelken@gmail.com
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